NTSB Meets on US Airways Airbus Flight 1549 Crash

The National Transportation Safety Board held a public Board meeting on May 4 on its investigation into the accident in which a US Airways jetliner came to rest in the Hudson River near New York City after a low-altitude encounter with a flock of birds.

The purpose of the meeting was to determine the probable cause of the accident and to consider proposed safety recommendations to reduce the likelihood of future such mishaps.

On January 15, 2009, at 3:27 p.m. EDT, US Airways flight 1549, an Airbus A320, lost engine power after striking a flock of Canada geese shortly after departing New York’s LaGuardia Airport. The captain brought the plane down into the Hudson River after determining that landing at an airport was not feasible. The plane, destined for Charlotte, N.C., carried 150 passengers and a crew of five. Four passengers and one flight attendant received serious injuries.

To supplement the facts discovered during the on-scene and subsequent follow-up investigation, the Safety Board held a three-day public hearing on this accident in June 2009. Transcripts, documents and other items from that hearing are available at:  http://www.ntsb.gov/events/2009/Weehawken-NJ/Default.html

The Board meeting was held in Washington on Tuesday, May 4, 2010, at 9:30 a.m. EDT, in the NTSB Board Room and Conference Center at 429 L’Enfant Plaza, S.W.

A live and archived webcast of the proceedings will be available on the Board’s website at http://www.ntsb.gov/Events/Boardmeeting.htm. Technical support details are available under “Board Meetings.” To report any problems, please call 703-993-3100 and ask for Webcast Technical Support. 

A summary of the Board’s final report, which will include its findings, probable cause and safety recommendations, will appear on the website shortly after the conclusion of the meeting. The entire report will appear on the website several weeks later.

NTSB Looks at Near-Crash over California

The National Transportation Safety Board has opened an investigation into the near collision of a commercial jetliner and a small private plane at the intersection of two active runways at Burbank’s Bob Hope Airport in Southern California.

At about 10:58 a.m. PDT on April 19, Southwest Airlines flight 649, a Boeing 737-700 (N473WN) inbound from Oakland, carrying 119 passengers and a crew of five was landing on runway 8 while a Cessna 172, in the departure phase of a “touch and go” on runway 15, passed over the 737.  A “touch and go” is a practice maneuver in which an aircraft briefly lands on the runway before accelerating and becoming airborne again.

According to the Federal Aviation Administration, the airplanes came within 200 feet vertically and 10 feet laterally of each other at the runway intersection. No one was injured in the incident, which occurred under a clear sky with visibility of 10 miles.

NTSB investigator Betty Koschig, an air traffic control specialist based in Washington, is traveling to Burbank today to begin the investigation.

Poor Maint Started Chain Resulting in Runway Crash

Washington, DC – A chartered business jet crashed at a South Carolina airport 18 months ago because of the operator’s inadequate maintenance of the airplane’s tires and the decision by the captain to attempt a high-speed rejected takeoff, which went against standard operating procedures and training, the NTSB determined today.

On September 19, 2008, at 11:53 p.m. EDT, a Bombardier Learjet Model 60 (N999LJ) operated by Global Exec Aviation and destined for Van Nuys, California, overran runway 11 during a rejected takeoff at Columbia Metropolitan Airport. After the airplane left the departure end of runway 11, it struck airport lights, crashed through a perimeter fence, crossed a roadway and came to rest on a berm. The captain, the first officer, and two passengers were killed; two other passengers were seriously injured.

The investigation revealed that prior to the accident the aircraft was operated while the main landing gear tires were severely underinflated because of Global Exec Aviation’s inadequate maintenance. The underinflation compromised the integrity of the tires, which led to the failure of all four of the airplane’s main landing gear tires during the takeoff roll.

Shortly after the first tire failed, which occurred about 1.5 seconds after the airplane passed the maximum speed at which the takeoff attempt could be safely aborted, the first officer indicated that the takeoff should be continued but the captain decided to reject the takeoff and deployed the airplane’s thrust reversers. Pilots are trained to avoid attempting to reject a takeoff at high-speed unless the pilot concludes that the airplane is unable to fly; the investigation found no evidence that the accident airplane was uncontrollable or unable to become airborne.

The tire failure during the takeoff roll damaged a sensor, which caused the airplane’s thrust reversers to return to the stowed position. While the captain was trying to stop the airplane by commanding reverse thrust, forward thrust was being provided at near-takeoff power because the thrust reversers were stowed. The Safety Board determined that the inadvertent forward thrust contributed to the severity of the accident.

The Safety Board also found that neither the Federal Aviation Administration nor Learjet adequately reviewed the Airplane’s design after a similar uncommanded forward thrust accident that occurred during landing in Alabama in 2001. While the modifications put into place after the Alabama accident provided additional protection against uncommanded forward thrust upon landing, no such protection was provided for a rejected takeoff.

“This accident chain started with something as basic as inadequate tire inflation and ended in tragedy,” said NTSB Chairman Deborah A.P. Hersman. “This entirely avoidable crash should reinforce to everyone in the aviation community that there are no small maintenance items because every time a plane takes off, lives are on the line.”

The safety recommendations that the NTSB made to the Federal Aviation Administration as a result of this investigation are: provide pilots and maintenance personnel with information on the hazards associated with tire underinflation, including the required intervals for tire pressure checks, and allow pilots to perform pressure checks in air taxi operations to ensure that tires remain safely inflated at all times; require tire pressure monitoring systems for all transport category airplanes; identify and correct deficiencies in both Learjet’s thrust reverser system safety analysis and the FAA’s design certification process to ensure that hazards encountered in all phases of flight are mitigated; require that simulator training for pilots who conduct turbojet operations include opportunities to practice responding to events other than engine failures near takeoff speeds; require that pilots who fly air taxi turbojet operations have a minimum level of pilot operating experience in an airplane type before acting as pilot-in- command in that type; and require that airplane tire testing criteria reflect the loads that may be imposed on tires both during normal operating conditions and after the loss of one tire.

A synopsis of the Board’s report, including the probable cause, conclusions, and recommendations, is available on the NTSB’s website, at http://www.ntsb.gov/Publictn/2010/AAR1002.htm. The Board’s full report will be available on the website in several weeks.

Cessna 152 Plane Crash Kills Pilot and Student

Investigators on Friday identified the bodies of a Scottsdale flight instructor and her student pilot who were killed when their small plane crashed into a mountain in the West Valley.

Officials said the instructor, Ondrea M. Benner, 34, of Scottsdale, and her student, Clint A. Bergum, 21, of Michigan, were the victims. Bergum was living in Phoenix but his primary residence was in Ypsilanti, Mich.

The wreckage of the single-engine Cessna 152 was spotted Thursday afternoon by a construction worker on a mountainside above the Quintero Golf & Country Club in Peoria. No one witnessed the crash, and the instructor and student were dead when emergency crews arrived, Peoria police spokesman Mike Tellef said.

Federal Aviation Administration records indicate Benner was issued a commercial pilot’s license in September 2003. FAA records also indicate she had been issued her flight instructor license two years ago as of June 26.

The aircraft belonged to the Pan Am International Flight Academy at Deer Valley Airport in Phoenix, Tellef said.

The academy referred calls to its corporate headquarters in Florida, which was closed Friday evening.

The cause of the crash is unknown. It will be investigated by the National Transportation Safety Board and the FAA.

SOURCE: Staff and Wire Reports

Learjet 35 Plane Crash

GROTON, Conn. — A Learjet 35 registered to religious broadcaster Pat Robertson crashed in Long Island Sound while flying in heavy fog Friday, killing both pilots, authorities said. All three passengers escaped without serious injury.

Robertson was not aboard.

The twin-engine Learjet 35 went down a half-mile short of the runway at Groton-New London Airport. Authorities said the passengers were able to get out on their own and were pulled from the water and taken to the hospital with minor injuries.

Preliminary information showed that the plane may have hit an approach light mounted in a cove near the airport, said Christopher Cooper, a spokesman for the state Department of Transportation.

SOURCE: CBS13

US Airways Express Flight 5481 Crash

On January 8, 2003, about 0847:28 eastern standard time, Air Midwest (doing business as US Airways Express) flight 5481, a Raytheon (Beechcraft) 1900D, N233YV, crashed shortly after takeoff from runway 18R at Charlotte-Douglas International Airport, Charlotte, North Carolina. The 2 flight crewmembers and 19 passengers aboard the airplane were killed, 1 person on the ground received minor injuries, and the airplane was destroyed by impact forces and a postcrash fire. Flight 5481 was a regularly scheduled passenger flight to Greenville-Spartanburg International Airport, Greer, South Carolina, and was operating under the provisions of 14 Code of Federal Regulations Part 121 on an instrument flight rules flight plan. Visual meteorological conditions prevailed at the time of the accident.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows: The airplane’s loss of pitch control during take-off. The loss of pitch control resulted from the incorrect rigging of the elevator system compounded by the airplane’s aft center of gravity, which was substaintially aft of the certified aft limit.

Contributing to the cause of the accident were (1) Air Midwest’s lack of oversight of the work being performed at the Huntington, West Virginia, maintenance station; (2) Air Midwest’s maintenance procedures and documentation; (3) Air Midwest’s weight and balance program at the time of the accident; (4) the Raytheon Aerospace quality assurance inspector’s failure to detect the incorrect rigging of the elevator control system; (5) the Federal Aviation Administration’s (FAA) average weight assumptions in its weight and balance program guidance at the time of the accident; and (6) the FAA’s lack of oversight of Air Midwest’s maintenance program and its weight and balance program.

SOURCE: NTSB